Interaction between AVR reactive power control and high power AC-DC converter control as possible cause of instability
Two oscillatory episodes took place in the Argentinean power system at 22:20 and 22:50, June 7th, 2008. The first one started when a 40 MVAr capacitors bank was disconnected and the second one started when a 500 kV line was disconnected. Both oscillatory episodes produced great variation of active a...
Guardado en:
Autores principales: | Agüero, Jorge Luis, Arnera, Patricia Liliana, Bianchi Lastra, Raúl E., Molina Milyus, Roberto D., Biteznik, Carlos Ezequiel, Barbero, Santiago |
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Formato: | Objeto de conferencia |
Lenguaje: | Inglés |
Publicado: |
2012
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Materias: | |
Acceso en línea: | http://sedici.unlp.edu.ar/handle/10915/36244 |
Aporte de: |
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